1-20 of 172 Search Results for

History/Category:1.3 Wellhead design

Follow your search
Access your saved searches in your account

Would you like to receive an alert when new items match your search?
Close Modal
Sort by
Proceedings Papers

Paper presented at the Abu Dhabi International Petroleum Exhibition & Conference, November 9–12, 2020
Paper Number: SPE-203207-MS
... designed. The collected data, ranging from 10 to 45 years of age, was highly fragmented and heterogeneous. For some wells, the missing information even included well construction files, cement logs, some overburden lithology parameters and, for one of the wells, the characteristics of wellhead and annulus...
Proceedings Papers

Paper presented at the SPE Offshore Europe, September 3–6, 1991
Paper Number: SPE-23145-MS
..., lands and locks onto the outside of the wellhead housing. Using a common subsea wellhead for the three proposed completions allowed major cost benefits in both the design and manufacturing phases of the subsea completion equipment. This conversion work was completed in the Spring of 1989. Well Status...
Proceedings Papers

Paper presented at the SPE Asia Pacific Oil and Gas Conference and Exhibition, September 9–11, 2003
Paper Number: SPE-80474-MS
... a specific work process covering well completion design, material selection, sand control, well flow modeling, completion fluids, cement evaluation, wellhead & Christmas trees, artificial lift, etc. 2 SPE 80474 by intensive re-development of matured fields and to venture out of Malaysia. These expansion...
Proceedings Papers

Paper presented at the Middle East Oil Show, June 9–12, 2003
Paper Number: SPE-81546-MS
... addition Steps in preparing the workflow consist of : - Preparing a high level work flow - Appointing each engineer to prepare a specific work process covering well completion design, material selection, sand control, well flow modeling, completion fluids, cement evaluation, wellhead & Christmas trees...
Proceedings Papers

Paper presented at the SPE International Improved Oil Recovery Conference in Asia Pacific, October 20–21, 2003
Paper Number: SPE-84916-MS
... on the production history shows that the decline was mainly due to the high and gradual increase of the flowing bottomhole pressure, which was possibly due to relatively high wellhead pressure (fluctuating between 25 to 40 atm according to the well reports) for the natural flow well, and the sporadic encroachment...
Proceedings Papers

Paper presented at the Offshore Technology Conference, April 30–May 3, 2018
Paper Number: OTC-28855-MS
...) supplier, Subsea Wellhead supplier, and Surface Wellhead/Tree supplier. Design and Interface Management play a significant role in the success of a project of this magnitude. The Shell Malikai Single Combo Casing Top Tensioned Riser (SCCTTR) was successfully deployed and commissioned on the first TLP...
Proceedings Papers

Paper presented at the SPE Middle East Intelligent Energy Conference and Exhibition, October 28–30, 2013
Paper Number: SPE-167421-MS
... and Stress Analysis Wellhead Design The Modular Zonal Management System (MZMS) was selected for the intelligent completion for well-A. The MZMS technology includes a specialized software module which is integrated into proprietary completion design software. This allows seamless integration...
Proceedings Papers

Paper presented at the Abu Dhabi International Petroleum Exhibition & Conference, November 13–16, 2017
Paper Number: SPE-188668-MS
.... The upper one joins up on the lower joint by cables from wellhead with help of gravity. Five flow holes of20mm diameter are assembly designed on the lower joint which unlocking mechanism stress is 1.2-2 t approximately. It achieves long-term stability, communications and power supply after docking...
Proceedings Papers

Paper presented at the Offshore Technology Conference, May 5–8, 2014
Paper Number: OTC-25403-MS
... and vessel-driven motions. A semi-analytical method was developed to estimate wellhead fatigue damage directly using the measured BOP stack motion data. High quality vibration data from the SVDLs were used in conjunction with analytical transfer functions to directly compute stress time histories and S-N...
Proceedings Papers

Paper presented at the SPE/IADC International Drilling Conference and Exhibition, March 8–12, 2021
Paper Number: SPE-204096-MS
... to 17.5 m used to date). Hence, the whole structure must be designed to withstand the entire well loads. This became a breakthrough in top-hole well design, because the risks involved in conductor running operations are avoided by integrating the low pressure wellhead housing (LPWHH) and the conductor...
Proceedings Papers

Paper presented at the SPE/ICoTA Coiled Tubing Roundtable, March 7–8, 2001
Paper Number: SPE-68427-MS
.... In most cases, the individuals operating the equipment have received the proper training and have adequate experience. Some important factors that negatively affect experience and judgment are distractions, monotone operations and fatigue. Case 1 In the Gulf of Mexico, a slim 1.3-in.-OD bottomhole...
Proceedings Papers

Paper presented at the 20th World Petroleum Congress, December 4–8, 2011
Paper Number: WPC-20-3330
... of transmission lines is not present. A typical offshore gas development is designed to deliver a relatively fixed quantity of gas into a pipeline system over a 24 hour period. This production, or supply-driven approach is designed to minimise changes to the wellhead choke positions within this period. Mismatches...
Proceedings Papers

Paper presented at the SPE/ICoTA Coiled Tubing Conference and Exhibition, April 8–9, 2003
Paper Number: SPE-81747-MS
... Completion Fluid (Type/SG) Sand Production Flow Rate Reservoir Temperature Reservoir Pressure Wellhead Pressure Well TVD Well MD Drag analysis Tubing and Casing Data During this initial well parameter review it is also determined if coiled tubing has been run in this well previously...
Proceedings Papers

Paper presented at the Low Permeability Reservoirs Symposium, March 6–8, 1989
Paper Number: SPE-18962-MS
... by increased volumes of undedicated reserves in the region and lower wellhead prices. Development History Development of the Moxa Arch area began in 1924 with the discovery of the La Barge oil field in Lincoln and Sublette Counties. Low permeability Frontier gas was discovered in the 1930's and 1940's...
Proceedings Papers

Paper presented at the SPE Hydraulic Fracturing Technology Conference and Exhibition, January 24–26, 2017
Paper Number: SPE-184851-MS
... 30% at an estimated 1.3 to 1.4% increase in well cost (based on cost of larger job sizes). Proppant mass had already been increased by the subject operator to 472 lbs/ft resulting in a 24% increase in one-year production in both formations compared to the mean of other operators in the AOI. Proppant...
Proceedings Papers

Paper presented at the International Petroleum Technology Conference, December 10–12, 2014
Paper Number: IPTC-18041-MS
..., which focused on the technical requirements of the project. Shell s Prelude project was the world s first project to take a Final Investment Decision on a FLNG facility. This happened in May 2011. Prelude FLNG is expected to produce 3.6 million tonnes per annum (mtpa) of LNG, 1.3 mtpa of condensate...
Proceedings Papers

Paper presented at the International Petroleum Technology Conference, November 14–16, 2016
Paper Number: IPTC-18801-MS
... with the gas lock situation. IPTC-18801-MS 5 Wellhead penetration system High pressure is one of the risks in gas wells, thus a reliable wellhead cable penetration system is necessary. The traditional pack-off method of penetration has been gradually replaced due to its poor reliability in high differential...
Proceedings Papers

Paper presented at the The Twelfth ISOPE Pacific/Asia Offshore Mechanics Symposium, October 4–7, 2016
Paper Number: ISOPE-P-16-007
... of Legs Monopod Brace Monopod Tripod 4 Legs 6 Legs Brace Configuration / - K - X Remaining Life x 4 4 < x 8 8 < x 12 12 < x 16 x > 16 Platform Function Process Service Wellhead Living Quarter Support The PoF scoring system is summarized in Table 1. Consequence of Failure (CoF) The CoF was used...
Proceedings Papers

Paper presented at the SPE Gas Technology Symposium, January 22–24, 1991
Paper Number: SPE-21484-MS
.... No gathering costs are included in the calculated wellhead price. First, we examined effect of uniform increases of fracture length with no reduction in cost-efficiency, to represent improved design and placement of fractures. Wells were modeled at 200, 400 and 600 foot effective lengths to determine...
Proceedings Papers

Paper presented at the SPE Latin American and Caribbean Petroleum Engineering Conference, April 27–30, 2003
Paper Number: SPE-81084-MS
...). Drilling History. Drilling commenced: 27-Apr-90 and terminated: 15-Dec-90. The well was drilled using clay mud, density 1.36 1.42 g/cm3 and viscosity 40 70 sec. All casings were cemented up to the wellhead with setting points as shown 6 SPE 81084 in the well schematic Figure 10. Cement column behind...

Product(s) added to cart

Close Modal