ABSTRACT
This paper summarizes the comprehensive reservoir characterization effort for the foam pilot area and discusses the response to foam injection in the CO2 Foam Field Verification Pilot Test conducted in the East Vacuum Grayburg San Andres Unit (EVGSAU) in New Mexico. A detailed study of the pilot pattern geology provided an understanding of the major controls on fluid flow in the foam pattern. Pattern performance data, falloff testing, profile surveys, and interwell tracer results were integrated into the geologic model to guide project design work and provide a framework for interpretation of foam performance. Localized regions of high permeability resulting from solution enhancement of the matrix pore system appear to be the primary cause of the early CO2 breakthrough and channeling of injected CO2 toward the problem production well in the foam pattern. Positive response to foam injection is indicated by reduced injectivity and injection profile data in the foam injection well; by results from time sequence monitor logging in the observation well; and by changes in production performance in the high GOR, "offending" production well in the foam pattern. Hall plots and pressure falloff testing were used to measure in situ changes in fluid mobility near the foam injection well. Time sequence logging responses at an observation well located 150 feet from the foam injector provided evidence of changes in fluid flow patterns in response to foam injection. Positive response to foam injection is further evidenced by changes in the C02 production and oil rate performance at the "offending" production well in the foam pilot pattern.