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Keywords: correction
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Proceedings Papers

Paper presented at the Annual Technical Meeting, June 7–10, 1997
Paper Number: PETSOC-97-43
... individual producing zone, reliable production information is needed. Any missing data should be filled in and allocation of commingled production should be checked and corrected if necessary. Such corrections were made to the available data for a reservoir simulation study of the Beda oil field. The Beda...
Proceedings Papers

Paper presented at the Annual Technical Meeting, June 6–8, 1995
Paper Number: PETSOC-95-01
... side of the business. better performance annual technical meeting different measure low margin fowlie petroleum society correction conclusion publication rights low growth area influence company operate canada producer key component competitive environment current trend...
Proceedings Papers

Paper presented at the Annual Technical Meeting, June 6–8, 1995
Paper Number: PETSOC-95-59
... mature field, with all twenty offsetting wells drilled and completed 14–15 years ago(the field was discovered over 18 years ago), the horizontal well had to answer several questions put forward by the Company: reservoir olanson upstream oil & gas directional drilling correction build...
Proceedings Papers

Paper presented at the Annual Technical Meeting, June 11–14, 1994
Paper Number: PETSOC-94-03
... the confidence limit contours can be derived. These are then used to draw correct inferences from the results - in the example, the possible communication between two oil pools is investigated. The 95% confidence limits are found to cover a wide range in the OOIP and gas cap fraction, thus the "best...
Proceedings Papers

Paper presented at the Annual Technical Meeting, June 11–14, 1994
Paper Number: PETSOC-94-82
... rectangle. For the estimation of an effective vertical permeability, no more than five to ten shales usually need to be included in a model. Correction factors can be applied to model the "real" shales as equivalent horizontal rectangles. The size of shale is a critical parameter in modelling a sand-shale...
Proceedings Papers

Paper presented at the Annual Technical Meeting, June 11–14, 1994
Paper Number: PETSOC-94-25
... was required to obtain the correct steady-state, Muskat analytical rate. This pressure does not correspond to the average pressure of the well block and generally requires changes to pressures obtained from pressure transient analysis for use in the simulator. In the method described here, it is found...
Proceedings Papers

Paper presented at the Annual Technical Meeting, June 11–14, 1994
Paper Number: PETSOC-94-19
... samples through removal of weighting material and correction for residual burite. The presented testing protocol eliminates volumetric measurements and replaces them with weight measurements which improve accuracy by an order of magnitude. The paper explains how to use results from dewaterability tests...
Proceedings Papers

Paper presented at the Annual Technical Meeting, June 11–14, 1994
Paper Number: PETSOC-94-26
... water cones into a vertical or horizontal well. A correction is applied to the simulator breakthrough times to incorporate the effects of numerical dispersion. The results obtained from the newly derived correlations are compared with existing analytical and numerical solutions for a number of cases...
Proceedings Papers

Paper presented at the Annual Technical Meeting, June 6–9, 1992
Paper Number: PETSOC-92-51
... Buckley-Leverett type analysis, which is based on the assumption of a stable and stabilized displacement, and to account for the presence of instabilities by using empirical sweep efficiency corrections. The relative permeabilities used in this type of analysis are usually obtained from laboratory tests...
Proceedings Papers

Paper presented at the Annual Technical Meeting, April 20–23, 1991
Paper Number: PETSOC-91-41
... & gas correction wellbore storage dual porosity HOW WELLBORE DYNAMICS AFFECT PRESSURE TRANSIENT ANALYSIS L. MATTAR M.S. SANTO this article begins on the next page F PETROLEUM SOCIETY OF CIM and AOSTRA PAPER NO. CIM / AOSTRA 91-41 ATM-17 THIS IS A PREPRINT - SUBJECT TO CORRECTION HOW WELLBORE...
Proceedings Papers

Paper presented at the Annual Technical Meeting, June 9–12, 1990
Paper Number: PETSOC-90-126
... correction reservoir simple analytical method directional drilling drilling operation permeability heavy-oil production upstream oil & gas petroleum society sparky sand singhal saturation sandstone pantella production performance horizontal well horizontal drilling regulatory bodies...
Proceedings Papers

Paper presented at the Annual Technical Meeting, January 1, 1989
Paper Number: PETSOC-89-40-12
... requires equal time interval shut-in periods. It has been recognized that the unstabilized rate and pressure leads to an overestimation of the well's deliverability potential; therefore, a final extended rate is required to make a correction to the unstabilized deliverability plot. This correction is made...
Proceedings Papers

Paper presented at the Annual Technical Meeting, June 7–10, 1986
Paper Number: PETSOC-86-37-17
... simulating effective overburden pressure (EOP) in a hydrostaticload cell and by measuring porosity and permeability as a function ofincreasing EOP. These data are typically corrected to uniaxial strainconditions to more closely represent reservoir confinement and correlationsbetween the ambient condition and...
Proceedings Papers

Paper presented at the Annual Technical Meeting, May 29–June 2, 1977
Paper Number: PETSOC-77-10
... capillary pressure permits a correction of the mercury intrusion porosimetry curve such that it gives the relationship between the neck diameter and the pore volume, the flow through which is controlled by that diameter. This correction is very significant (about 50 volume %) near the threshold capillary...
Proceedings Papers

Paper presented at the Annual Technical Meeting, June 10–12, 1975
Paper Number: PETSOC-75-21
... behaved like pseudoplastic fluids. Apparent viscosity or consistency increased with the concentration of the dispersed phase and decreased with temperature. ASTM plots of kinematic viscosity vs temperature were linear for each emulsion. Viscosity corrections for temperature could be made for the W/O...

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